X-Git-Url: http://git.monstr.eu/?a=blobdiff_plain;f=arch%2Farm%2Fboot%2Fdts%2Fimx6qdl-sr-som.dtsi;h=f86efd0ccc4047021662011948b9a593ea872643;hb=befa491ce6954adadb181c464d0318925f18e499;hp=0ad8ccde0cf87414e08be60e6ba880d02ed0ba3d;hpb=a727df407ca4f9bc0e9c30b7b469fc990a235be3;p=linux-2.6-microblaze.git diff --git a/arch/arm/boot/dts/imx6qdl-sr-som.dtsi b/arch/arm/boot/dts/imx6qdl-sr-som.dtsi index 0ad8ccde0cf8..f86efd0ccc40 100644 --- a/arch/arm/boot/dts/imx6qdl-sr-som.dtsi +++ b/arch/arm/boot/dts/imx6qdl-sr-som.dtsi @@ -54,7 +54,13 @@ pinctrl-names = "default"; pinctrl-0 = <&pinctrl_microsom_enet_ar8035>; phy-mode = "rgmii-id"; - phy-reset-duration = <2>; + + /* + * The PHY seems to require a long-enough reset duration to avoid + * some rare issues where the PHY gets stuck in an inconsistent and + * non-functional state at boot-up. 10ms proved to be fine . + */ + phy-reset-duration = <10>; phy-reset-gpios = <&gpio4 15 GPIO_ACTIVE_LOW>; status = "okay";